Oil Filter Adapter o-ring
#64
::CF Moderator::
Joined: Sep 2009
Posts: 3,333
Likes: 381
From: Glen Burnie, MD
Year: 2001
Model: Cherokee (XJ)
Engine: 4.0l
Handy website, it provides all the cross numbers.
Last edited by Veeb0rg; 01-01-2012 at 11:00 AM.
#65
Junior Member
Joined: Mar 2010
Posts: 91
Likes: 0
From: Reno, NV
Year: 1996
Model: Cherokee
Engine: 4.0 6 cyl
hiting engine support
greeting from planet MS. I have a 94 cherokee sport. great site and lots of helpful info. I need to fix a leak in the OFA. Three, o-ring kit needed and some elbow grease. Oil changing place told me i had a cracked thread or some bull cockie, after reading on here I suspect the o-rings need replacing. Does not look fun though. Before I start any other suggestions or processes? I found this site while searching the forum:
POSTED BY REWSTER, SEP 8TH, WWW.CHEROKEEFORUM.COM/SHOWTHREAD.PHPT=1385.
Any other advice?
Thanks in advance!!!
POSTED BY REWSTER, SEP 8TH, WWW.CHEROKEEFORUM.COM/SHOWTHREAD.PHPT=1385.
Any other advice?
Thanks in advance!!!
Rewster,
Yes, I posted about completly eliminating the 90 deg adapter and o-ring because it will go out again, I still have an oil spot from a year ago. The taking the hollowbolt from adaptor, going straight into the block then simply spining on an oil filter (smaller OF to fit) does work.
I have had one problem after 20,000 miles. I go down a 2/3 mile 2,000' drop trail, rather frequently and with 178k the engine mounts are soft and the engine goes forwardand dents the OF with the engine mount supprt. On mine a 3/8" gap.
With Fram it never leaks but with Purolator extra duty 99% OF it did open a leak in OF case as guess since better with metal endcaps inside the purolator case can not dent as much and it did develope a split.
Unfortanately it is very hard to get to that spot to grind back the frame support another 1/4" which would have no effect on strength, its just extra metal. So I rounded it with file. Just had this problem.
My plan is to put a poly engine mount in so it does not shift as much. or if anyone has another idea to prevent enging from shifting forward?
So check yours for clearance. You can do teh swap without losing teh ability to go back to adaptor at no cost, just swap the hollow bolt back.
#66
Member
Joined: Oct 2010
Posts: 147
Likes: 0
From: NJ / Tuscaloosa
Year: 2000
Model: Cherokee
Engine: N/A
Hey guys, do you think something like this is an option?
http://www.jegs.com/i/JEGS+Performan...51715/10002/-1
http://www.jegs.com/i/JEGS+Performan...51715/10002/-1
#67
Junior Member
Joined: Mar 2010
Posts: 91
Likes: 0
From: Reno, NV
Year: 1996
Model: Cherokee
Engine: 4.0 6 cyl
Remote mount
Hey guys, do you think something like this is an option?
http://www.jegs.com/i/JEGS+Performan...51715/10002/-1
http://www.jegs.com/i/JEGS+Performan...51715/10002/-1
If you go that far maybe you want to add a oil cooler while at it.
#68
Great thread! and great idea Darp! Now to figure out where to mount the coolers (I would do a trans cooler too) Maybe tucked up under my winch bumper!
Every time I read one of these great threads it cost me money. Oh well, I am so far ahead selling my Mini Cooper S and getting an XJ. The XJ also keeps me in the shop and out of the house .......
This looks like it might fit the bill and does trans and engine cooler with remote filter.
http://www.summitracing.com/parts/SUM-G4978/
Every time I read one of these great threads it cost me money. Oh well, I am so far ahead selling my Mini Cooper S and getting an XJ. The XJ also keeps me in the shop and out of the house .......
This looks like it might fit the bill and does trans and engine cooler with remote filter.
http://www.summitracing.com/parts/SUM-G4978/
Last edited by RShrimp; 01-05-2012 at 08:24 AM.
#69
For those with a welder, making a tool is a cinch and surprisingly it doesn't take as much force as those have suggested. I swapped mine out last night and only added 20 some od mins to my regular change time. I would like to note that my '97 had zero loc-tite residue on the threads. I see no reason to loc-tite it and outside making a tool, this job is incredibly easy to do. I don't see a good reason to remove the adapter, they don't leak THAT often. Just fix it and worry about it in another 100k miles; lol.
I bought a T60 that was pressed into a 1/2" drive socket. Using a 4" cutting wheel, I split the drive socket and used and arbor press to remove the T60 bit. Then welded it to the end of some 5/8" bar stock @~18" long. Broke it free from the bottom and never needed to disconnect the starter.
I bought a T60 that was pressed into a 1/2" drive socket. Using a 4" cutting wheel, I split the drive socket and used and arbor press to remove the T60 bit. Then welded it to the end of some 5/8" bar stock @~18" long. Broke it free from the bottom and never needed to disconnect the starter.
Last edited by s14unimog; 01-13-2012 at 12:56 PM.
#70
CF Veteran
Joined: Dec 2011
Posts: 3,237
Likes: 1
From: albany, new york
Year: 1988
Model: Cherokee
Engine: i6
bump, cause if you spend the extre $1.20 you can get some nice brown, viton orings that are designed for corrosive materials and higher temps...it may be like $2.40 but it will outlast your jeep, reg orings will be fine cause engine oil is not corrosive, but high temp/ viton wont hurt...
#71
"regular", which is likely buna, is resistant to a lot more than "non-corrosives" but you're right about a higher temperature operating range. Most Viton's are good to 350*F and above, while Buna is only good to ~ 250*F
My concerns are getting the exact specs of the required o-rings to source the viton ones.
My concerns are getting the exact specs of the required o-rings to source the viton ones.
#72
Newbie
Joined: Jan 2011
Posts: 24
Likes: 0
From: Torrance CA
Year: 1996
Model: Cherokee
Engine: 4.0L HO
Replaced the leaky adapter O ring today - used the Torx key set from O Reilly's and a jack handle for more leverage on the T-60, used the T-55 for the last few turns. Old O ring had gone hard and stuck to the engine block - greased the new ring to stop it falling out, I didnt remove the filter.
Thanks for the advice from everyone on here.
Ian
Thanks for the advice from everyone on here.
Ian
#73
Junior Member
Joined: Mar 2010
Posts: 91
Likes: 0
From: Reno, NV
Year: 1996
Model: Cherokee
Engine: 4.0 6 cyl
Better Oil Filter to eliminate Adaptor, WIX 51348
Rewster,
Yes, I posted about completly eliminating the 90 deg adapter and o-ring because it will go out again, I still have an oil spot from a year ago. The taking the hollowbolt from adaptor, going straight into the block then simply spining on an oil filter (smaller OF to fit) does work.
I have had one problem after 20,000 miles. I go down a 2/3 mile 2,000' drop trail, rather frequently and with 178k the engine mounts are soft and the engine goes forwardand dents the OF with the engine mount supprt. On mine a 3/8" gap.
With Fram it never leaks but with Purolator extra duty 99% OF it did open a leak in OF case as guess since better with metal endcaps inside the purolator case can not dent as much and it did develope a split.
Unfortanately it is very hard to get to that spot to grind back the frame support another 1/4" which would have no effect on strength, its just extra metal. So I rounded it with file. Just had this problem.
My plan is to put a poly engine mount in so it does not shift as much. or if anyone has another idea to prevent enging from shifting forward?
So check yours for clearance. You can do the swap without losing the ability to go back to adaptor at no cost, just swap the hollow bolt back.
Yes, I posted about completly eliminating the 90 deg adapter and o-ring because it will go out again, I still have an oil spot from a year ago. The taking the hollowbolt from adaptor, going straight into the block then simply spining on an oil filter (smaller OF to fit) does work.
I have had one problem after 20,000 miles. I go down a 2/3 mile 2,000' drop trail, rather frequently and with 178k the engine mounts are soft and the engine goes forwardand dents the OF with the engine mount supprt. On mine a 3/8" gap.
With Fram it never leaks but with Purolator extra duty 99% OF it did open a leak in OF case as guess since better with metal endcaps inside the purolator case can not dent as much and it did develope a split.
Unfortanately it is very hard to get to that spot to grind back the frame support another 1/4" which would have no effect on strength, its just extra metal. So I rounded it with file. Just had this problem.
My plan is to put a poly engine mount in so it does not shift as much. or if anyone has another idea to prevent enging from shifting forward?
So check yours for clearance. You can do the swap without losing the ability to go back to adaptor at no cost, just swap the hollow bolt back.
Also on preventing the engine from surgeing forward, can see a solution. There is a heavy stamped metal covering over the motor mount, that does the mounting. If you were to drill 2-3 holes through it, lets say for 1/4" or 5/16" self tapping bolts, which bolts an additional plate that can be bolted on top that would go rearward to within 1/4" of where engine part that the MM bolt goes through. That way the engine can only surge forward 1/4" before it hits, protecting the new location of the oil filter which has about 1/2" clearance.
Last edited by darp; 02-18-2012 at 11:20 AM. Reason: spelling, and update
#74
Junior Member
Joined: Mar 2010
Posts: 91
Likes: 0
From: Reno, NV
Year: 1996
Model: Cherokee
Engine: 4.0 6 cyl
For those with a welder, making a tool is a cinch and surprisingly it doesn't take as much force as those have suggested. I swapped mine out last night and only added 20 some od mins to my regular change time. I would like to note that my '97 had zero loc-tite residue on the threads. I see no reason to loc-tite it and outside making a tool, this job is incredibly easy to do. I don't see a good reason to remove the adapter, they don't leak THAT often. Just fix it and worry about it in another 100k miles; lol.
I bought a T60 that was pressed into a 1/2" drive socket. Using a 4" cutting wheel, I split the drive socket and used and arbor press to remove the T60 bit. Then welded it to the end of some 5/8" bar stock @~18" long. Broke it free from the bottom and never needed to disconnect the starter.
I bought a T60 that was pressed into a 1/2" drive socket. Using a 4" cutting wheel, I split the drive socket and used and arbor press to remove the T60 bit. Then welded it to the end of some 5/8" bar stock @~18" long. Broke it free from the bottom and never needed to disconnect the starter.